Holland board build

@Marc87 ,

https://efoil.builders/uploads/default/original/2X/4/4e2d6dadb657d4c56e0c3d871cb70eb5c9bb7a8e.jpeg

Thanks Manu, will study this!

It’s been quite for a while, but I have been working plenty of hours on the project. Especially the board, close to a never ending story of sand paper, epoxy and filler, and again and more. But the last 2 weeks the board took some shape.

I epoxied my hatch frame into the board, using a mixture of epoxy and a small cotton fibres, to thicken the paste. The wooden hatch was placed on top to create an even pressure on the 3d printed frame. The small gap between the frame and the board was filled with more epoxy. Really hope this is properly water tight.

The steel counter plate with long studs fixed to the fin boxes was also installed and tightened securely. I used metal pipes around the studs between the metal plate and the fin box in order to avoid compression/denting the foam board. It feels quite sturdy. I used a polyurethane foam to fill the hole. So can’t access it anymore.

I left the original glass fibre structure intact wherever I could, but in order to compensate for the Ebox hole I added a layer of fibre glass in the E-box and on the top+bottom of the board. Wooden strips + fibre class were epoxied into the bottom of the board earlier.

Against the backside of the box you see a 3d printed plate+frame. This “collector” is where the motor wires + waterline come from the mast. The collector is epoxied for water tightness and then heavily gloed into the board, to avoid leeks. I will place the cable glands into the red cover plate once the cables are pulled and finally epoxy this into place as well.

I am quite afraid that the box might not be fully water tight so I designed a polycarbonate box to go inside the box. All the electrics will be installed into the polycarbonate box and some additional cable glands will wire the cables outside this box.
Unfortunately the company did not provide all the parts, so could only glue half the box together.
I guess apart from designing, fabricating parts, overcoming challenges, etc waiting is big part of this project :smiley:

But it is all slowly coming together. Yesterday night if secured the efoil to my custom board for the first time. It does all get quite heavy, have to check the weight, very curious.

Next step is to paint the board. Unfortunately for me 1m above my head here I have neighbours, and poorly insulated floors, who complained about me painting before. So I have to make a paint booth in my guest bedroom.
I soldered all the electrics together and powered the prop with 12S, feels very powerful. So soon I can assemble the motor pod and pull the wires into the board.
Then finalising the poly carbonate box + some other small bits in pieces.
Half May is the target for first testing. Keeping my fingers crossed

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I have almost the same shape of board. Mine is only 135cm long and 77cm wide but it works very well. My weight is 73kg.

Cool, sounds promising for me. My weight is about 70 with roughly same volume of the board.

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Last couple of weeks I tried to finalize the Propellor pod design. Really afraid that seals will leak because of the mismatch between propshaft and coupler.
Tried a few designs and printed a few new sealmounts to test. Below proposal is based upon a Hiorth setup using jaw type coupler. But I had some issues to make the custom shaft or having it made turned out very expensive.


Next option was with a much larger clamp coupler and redesigning the PM sealmount so it would fit this coupler. Thought it would be good to add a second (dry) bearing and have quite a big gap between seals which I will fill with grease. I also increased the length a bit so a grub screw can be placed before the O-rings. My solidworks skills improve because of all this quite a bit :slight_smile:

Today the coupler finally came, and it is quite a unit, 40mm long with two clamping screws per shaft.
So an important moment, would the shaft (by now 130mm) fit properly and will er be less to no wobble during operation. I did not add the second dry bearing yet but what a difference! Below current setup in a nutshell.


I probably will tried the jaw coupler eventually as well, but I’m building for 9months now and want to get onto the water :smiley:

Board and Electric box are pretty much finished. Just need final positioning of the ESC and pump/display mount.
The E-box is a box in a box. So a bit weird, but have 2 lines of glands to get cables into the board. Water tightness test 1 was positive and increased it a bit further with the rubber seals ontop of the box (visible below).
The batteries a secured with Velcro and this seems to work very nicely. A rubber strip is mounted to the inner polycarbonate box side walls. So hope the lid seals even better now.
I plan to assemble the Prop pod this weekend and pull the wires in. Lets see how it goes.

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Congrats on the build, looks good. Your big coupler looks similir to mine, Ruland stainless, quite big. Mine has a slot for a key which prevents slip (a common problem when using a coupler). Due to the lenght of the coupler, the shaft alligns quite well, 5/100 untrue at the pod exit of the shaft in my case. I don‘t know how much wobble other builders have, would be interresting to see if you have a dial gauge.The coupler should be balanced to reduce vibration. I removed matrrial with an angle grinder until it was balanced.

Thanks @sat_be Daniel. I have a non branded one, but think will work same as yours. I haven’t measured the untrue value for my setup, as I don’t have a dial gauge. Might ask around if somebody has this laying around. Eye balling it so far and looks promising. Leaks at the seals are one of my big worries.
Good point regarding the balancing, will check it out. How did you test this?

Put a shaft through it and put it on 2 parallel bars (shaft on the bars, coupler in the air). It will turn to the position with the heavyest point to the down side. (The side opposite of the screws). Mark it and remove some material with an angle grinder. Repeat until it keeps the position. You can also see it in the way it mooves when you create a (very flat) slope with the parallel bars and let it roll down. Only remove small portions, don‘t remove too much.

Thanks Daniel, very clear. I actually read about it for RC props, logical to use it for this purpose as well. Going to try it out.

Worked the whole weekend to finalise the board. I think i am sort of there :slight_smile:

I pulled the motor wires + water cooling line into the board and secured the mast to the board.
It actually fits in the car, only requires to disconnect the fuselage + prop&duct.

Up next was to hook up all the wires in the E-box. Quite a bit of work and I hope my soldering holds up. Working half standing with clamp and soldering iron over the box was a bit tricky.
Tested the motor a lot and it works great so far. The dead-mans switch also works good in dry condition and “loosing connection” with the remote also switched of the motor. I hope its ready

What’s left is grease the seals of the wooden lid, securing the rear foil and getting a wet suit. The batteries are all charged up. And so am I. I feel very excited and a little anxious as well. Hope it doesn’t go up in smoke!

Next: actually going into the water, hope I can bring some positive news :smiley:

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Water “shoes” and suit , help for the knees the first time ( getting on and on the board a few time …)

Yes, the water shoes also. I have those from wind surfing. Did you also added the “grip” on the board itself (don’t know what it is called)?
Good tip, will try it out like that :slight_smile:

“Pad” i think
https://gongsupshop.com/epages/box1707.mobile/fr_FR/?ViewAction=View&ObjectID=669266&PageSize=5&Page=3

https://www.hydroturf.com/hydro-requestsup

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Haha go for it Marc. I know the feeling so well. It can go wrong, or it is party time with a big smile at the water :smile:

€ 8,47 6%OFF | Srfda 18003205mm Surfboard deck pad daimond line FR EVA Dek grip heeft lijm sup dek pad in surfen Skiën sport
https://s.click.aliexpress.com/e/1NzRcqi8x

I use this

Thanks Louis. It is exciting!

I tested the board in the water for the first time.
It is really water proof so far, I am mostly happy about that. I made a few test runs laying on the board, so cool!! But I kicked of the deadmans switch which fell in the water and disappeared haha. So 5 minutes and that was it for now. But it is working :smiley: I will be back soon

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Well these were some expensive weeks and hard learned lessons.

Burned my Seaking ESC because one of the phase wires got detached in the motor pod. I thought to be smart and use the existing connectors. But no, bad idea! Ordered a Flier 320 and got that 1,5 week ago. Build up the pod, soldered the phase wires this time, and pulled the wires into the E-box last week and was ready for a new try last Friday.

Got into the water and did literally 1 run before I lost power. Motor still worked, it seemed. Back on land I touched the pod and it was very very hot.
Once in the garage I had no reaction of the engine at all so decided, without further ado, to cut the alu pipe. I found my whole phase cabling in a big spagetti. What the heck. Well, I forgot to use the grubscrews in the sealmount/alu pipe to avoid rotation of the engine in the pod!!! That’s what you get when you are too enthusiastic to go into the water I guess… I checked my checklist and noticed it wasn’t there. I guess last time I added it in the moment but forgot it this time :frowning:

So ordered a now motor as well and expanded my checklist. 3d printer is making over hours again, to the delight of my girlfriend.

Good thing is that everything else, also the engine pod, was still dry.

Also the prop seems crazy powerful, Its lifting me with the slightest movement of the trigger. Will try with a different prop next time.

Hope to be back in the water in 2 weeks.

Hi Mark, thanks for sharing your experiences… the good and the bad :slight_smile:
Where do you ride in Holland? I’ve started my build this month, planning to fly end of this summer near Leiden/Alphen.

I read a lot about a forklift relay to cut the power to the esc if you fall. But I’m not sure if this is a good idea? In my swordfish manual they say you can’t cut the power when the motor is running. I think it is better to only cut the receivers power? Also you don’t need a big relay for this. What do you guys think?

Here also from Holland, Drenthe. With my build I also planned a full cut off power. To be sure everything is off. I think it is more safe. And you wont cut off under load. The remote control goes to 0 % throttle. But just in case something goes wrong I want to be sure I will loose all battery power. With a magnet switch to a board leash and a 200a relay inside.